Abstract:In this study, the authors experimentally investigate the performance of the organic Rankine cycle (ORC) and screw expander under the influence of supply pressure and pressure ratio over the expander. Three tests were performed with expander pressure ratios of 2. 4-3.5, 3.0-4.6, and 3.3-6.1, which cover the over-expansion and under-expansion operating modes. The test results show a maximum expander isentropic efficiency of 72.4% and a relative cycle efficiency of 10.5% at an evaporation temperature of 101 °C and condensation temperature of 45 °C. At a given pressure ratio over the expander, a higher supply pressure to the expander causes a higher expander isentropic efficiency and higher cycle efficiency in the over-expansion mode. However, in the under-expansion mode, the higher supply pressure results in a lower expander isentropic efficiency and adversely affects the cycle efficiency. The results also show that under the condition of operation at a given pressure ratio, a higher supply pressure yields a larger power output owing to the increased mass flow rate at the higher supply pressure. The study results demonstrate that a screw-expander ORC can be operated with a wide range of heat sources and heat sinks with satisfactory cycle efficiency.
An organic Rankine cycle system comprised of a preheater, evaporator, condenser, turbine, generator, and pump was used to study its off-design performance and the operational control strategy. R245fa was used as the working fluid. Under the design conditions, the net power output is 243 kW and the system thermal efficiency is 9.5%. For an off-design heat source flow rate (m W ), the operating pressure was controlled to meet the condition that the R245fa reached the liquid and vapor saturation states at the outlet of the preheater and the evaporator, respectively. The analytical results demonstrated that the operating pressure increased with increasing m W ; a higher m W yielded better heat transfer performance of the preheater and required a smaller evaporator heat capacity, and the net power output and system thermal efficiency increased with increasing m W . For the range of m W studied here, the net power output increased by 64.0% while the total heat transfer rate increased by only 9.2%. In summary, off-design operation of the system was examined for a heat source flow rate which varied by -39.0% to +78.0% from the designed rate, resulting in -29.2% to +16.0% and -25.3% to +12.6% variations in the net power output and system thermal efficiency, respectively.
OPEN ACCESSEnergies 2014, 7 3685
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