The application of hydroponic cultivation fertilized with biologically nitrified synthetic urine can produce nitrate-rich fertilizer for lettuce (Lactuca sativa var. capitata L.). The mounting water crisis and depletion of natural resources makes nitrogen recovery from human urine a practical option. Nitrified urine can be used in indoor vertical hydroponic cultivation and is characterized by a high degree of element recovery. Because of its high ammonium content, hydrolyzed fresh urine may be toxic. A nitrification sequencing batch reactor with suspended activated sludge biomass ensured urine stabilization and biological conversion into nitrate-rich fertilizer. The diluted nitrate-rich fertilizer was then supplied for soilless cultivation. The results show that diluted nitrified urine is an excellent source of bioavailable nitrogen and phosphorus and, with proper enrichment with microelements, could replace commercial fertilizers in hydroponic systems. The yield and quality parameters of lettuce cultivated with enriched urine were comparable to those obtained with a commercial fertilizer. The mass balance calculation showed that industry-scale lettuce production can be based on urine fertilizer collected from a few hundred people for a single unit.
The anammox process is an economically favourable nitrogen removal process; however, low growth rates of anammox biomass block its more widespread application. As different approaches on techniques for anammox bacteria growth acceleration were tested, this study focused on long-term evaluation of hydrazine addition in the start-up phase. Effect of hydrazine addition (dose 3.7 mgN 2 H 4 dm −3 ) was investigated in a pilot-scale SBR treating ammonia-rich reject water from sludge dewatering after partial nitritation process, and effects were compared to a reference reactor. Hydrazine addition resulted in much higher anammox biomass enrichment observed as higher nitrogen removal rate [0.512 kgN (m 3 d) −1 with hydrazine versus 0.256 kgN (m 3 d) −1 without reagent]. Sludge from chemically stimulated reactor revealed also higher (by 22.6%) specific anammox activity rate than the reference. After the hydrazine addition was stopped, observed process rates remained stable and no regression in the nitrogen removal efficiency could be noticed. In the final phase, nitrogen removal rate was only 48.7% of process rate in the reactor previously stimulated by hydrazine. Results of the experiment confirmed positive effect of hydrazine presence on anammox bacteria enrichment process.
Stable and efficient nitrogen removal is one of main goals of wastewater treatment. Applying deammonification, beyond many advantages, results in the risk of the WWTP effluent quality violation in case of the failure of the process. Then nitrogen load to activated sludge is increasing rapidly which could therefore lead to quality violation in activated sludge effluent. Simulation studies have been presented on the effect of deammonification failure on nitrogen removal performance in the case of a typical, medium sized WWTP (ca. 115 000 PE). The studies were based on the calibrated ASM1 model of real WWTP and a fictional scenario of implementing deammonification and subsequent failure. Implementing deammonification enables SRT optimization of the sludge retention time (SRT) in its main line thanks to lower nitrogen load. Two scenarios have been shown, considering or not optimization of the SRT in WWTP. The results show that SRT optimization leads to decrease in nitrifier mass and raises difficult issues in appropriate nitrogen concentration in the effluent.
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