Day 2 Tue, November 16, 2021 2021
DOI: 10.2118/207834-ms
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The Root Cause Analysis and Successful Control of an Oilwell Blowout in the Middle East

Abstract: In 2017, a blowout and explosion occurred in a drilling oilwell in the Middle East. After drilling to the depth of 2,610 m, tripping was decided in order to change the bit. When the crew were pulling the drill string out of the hole with the drill-string being at the depth of 1332 m, blowout and explosion occurred. The well was a development well drilling almost horizontally (82 degrees inclination angle) into a highly-pressured gas-cap and oil pay-zone of the oilfield. In this work, following a brief explanat… Show more

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Cited by 3 publications
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“…After the initial kick response and the formation flow are stopped, a kick must be circulated out of the well to allow ordinary operations to resume (Ashena et al, 2021). To prevent more kicks, the kick must be cycled to the surface while the wellbore pressure is kept constant.…”
Section: Driller's Methodsmentioning
confidence: 99%
“…After the initial kick response and the formation flow are stopped, a kick must be circulated out of the well to allow ordinary operations to resume (Ashena et al, 2021). To prevent more kicks, the kick must be cycled to the surface while the wellbore pressure is kept constant.…”
Section: Driller's Methodsmentioning
confidence: 99%