2016
DOI: 10.1016/j.biortech.2016.07.061
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Effects of sludge retention time on oxic-settling-anoxic process performance: Biosolids reduction and dewatering properties

Abstract: Nghiem, L. D. (2016). Effects of sludge retention time on oxic-settlinganoxic process performance: biosolids reduction and dewatering properties. Bioresource Technology, 218 1187-1194.Effects of sludge retention time on oxic-settling-anoxic process performance: biosolids reduction and dewatering properties AbstractIn this study, the effect of sludge retention time (SRT) on oxic-settling-anoxic (OSA) process was determined using a sequencing batch reactor (SBR) attached to external aerobic/anoxic reactors. The … Show more

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Cited by 38 publications
(30 citation statements)
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“…The specific oxygen uptake rate (SOUR) slightly increased from Period 1 (30 mgO2 L -1 h -1 ) to Period 3 (31.7 mgO2 L -1 h -1 ), whereas it significantly arose in Period 4 to approximately 40 mgO2 L -1 h -1 . The SOUR increase was previously observed in OSA systems (Semblante et al, 2016b). The sharp increase of SOUR was likely related to the alternation of fasting/feasting conditions, which led the starved biomass to use more oxygen when it was returned to the mainstream aerobic reactor where a high substrate availability was ensured by the influent wastewater.…”
Section: Behavior Of Oho and Paos Kineticssupporting
confidence: 56%
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“…The specific oxygen uptake rate (SOUR) slightly increased from Period 1 (30 mgO2 L -1 h -1 ) to Period 3 (31.7 mgO2 L -1 h -1 ), whereas it significantly arose in Period 4 to approximately 40 mgO2 L -1 h -1 . The SOUR increase was previously observed in OSA systems (Semblante et al, 2016b). The sharp increase of SOUR was likely related to the alternation of fasting/feasting conditions, which led the starved biomass to use more oxygen when it was returned to the mainstream aerobic reactor where a high substrate availability was ensured by the influent wastewater.…”
Section: Behavior Of Oho and Paos Kineticssupporting
confidence: 56%
“…of sludge reduction was obtained in a SBR connected to an anaerobic side stream reactor operating under 12 h of HRT and 30 days of SRT (Semblante et al, 2016b). In another study carried out with ASSR-MBR systems, the maximum excess sludge reduction (55-58%) was achieved under 10-11 h of HRT in the anaerobic reactor (Saby et al, 2003;Ferrentino et al, 2016).…”
Section: Biomass Growth and Excess Sludge Productionmentioning
confidence: 92%
“…The reactors used in this study were previously described (Semblante et al, 2016). Briefly, the OSA system consisted of a sequencing batch reactor, SBROSA (5 L), attached to external aerobic/anoxic (2 L) and anoxic reactors (2 L) ( Figure 1a).…”
Section: Reactor Configuration and Operationmentioning
confidence: 99%
“…Sludge reduction was determined as described in a previous study (Semblante et al, 2016). Briefly, sludge reduction was the difference in sludge yield of SBROSA and SBRcontrol:…”
Section: Sludge Reductionmentioning
confidence: 99%
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