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2002
DOI: 10.1109/41.993263
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Design and loss comparison of matrix converters, and voltage-source converters for modern AC drives

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Cited by 142 publications
(42 citation statements)
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“…Not all the possible combinations of switches are allowed, they are restricted to only 27 valid switching states. As mentioned earlier the main advantage of matrix converter is the reduction in size being specially suited for automotive and aircraft applications [52] [53].…”
Section: Direct Convertersmentioning
confidence: 99%
“…Not all the possible combinations of switches are allowed, they are restricted to only 27 valid switching states. As mentioned earlier the main advantage of matrix converter is the reduction in size being specially suited for automotive and aircraft applications [52] [53].…”
Section: Direct Convertersmentioning
confidence: 99%
“…Wheeler et al investigated in 1994 the relative cost of two different input filter topologies for MCs (166) and suggested in 1997 an optimized input filter design for MCs using a one-stage LC input filter with harmonic diversion (167) . In 2002, Bernet et al computed the total conducted noise of a CMC and compared it with the results for a corresponding VSC (168) . One year later, Cha and Enjeti suggested a novel modulation method for MCs to reduce the generated common mode voltage (169) .…”
Section: Input Filters and Emcmentioning
confidence: 99%
“…Bernet et al presented in 2002 a comparison of the semiconductor losses and the design including a computation of the conducted noise (EMC) between the CMC and V-BBC (168) . In the same year, Zhou et al from Rockwell Automation investigated the critical operating points and their impact on the semiconductor design of CMCs from a drive manufacturer's perspective (175) and nicely summarized the key properties of the CMC in respect of the industrially widely applied V-BBC.…”
Section: Comparisons With Other Topologiesmentioning
confidence: 99%
“…However to achieve good dynamics, reasonable costs, weight and losses, the inductance should be around or less then 0.1 pu in real realization. For the IEEE 519-1992 limitations and the assumption that i ripple,peak not exceeds 10% (2.3A) the converter side, inductance L1, implemented with iron powder core, can be calculated to be [16]:…”
Section: Lcl Filter Designmentioning
confidence: 99%