The various factors considered in recommending the initiation of a gas injection project in the southern portion of the Cedar Lake Field are discussed. Performance history under gas injection operations is reviewed and these data are analyzed, utilizing both the material balance method and the fractional flow and frontal advance expressions.Results of the analysis of the performance data indicate that the injected gas has contacted and affected at least 60 per cent of the reservoir and a substantial increase in ultimate recovery can reasonably be expected. By holding the reservoir pressure appreciably above the bubble point, the well productive capacities have been maintained substantially above the level predicted for primary operations.The analysis of the Cedar Lake project suggests that in certain limestone reservoirs, at least, the probable success of gas injection cannot be predicted simply from observation of permeability distribution throughout the pay section, as indicated by core analysis data, on either one or a number of wells. Further, the performance of this particular project fails to indicate any basis for classifying carbonate reservoirs in general as being inherently unsuited to a dispersed type gas injection program, thus indicating that each reservoir should be considered on its own merits, regardless of the composition of the reservoir rock.
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