The tip leakage flow characteristics for flat and squealer turbine tip geometries are studied in the von Karman Institute Isentropic Light Piston Compression Tube facility, CT-2, at different Reynolds and Mach number conditions for a fixed value of the tip gap in a nonrotating, linear cascade arrangement. To the best knowledge of the authors, these are among the very few high-speed tip flow data for the flat tip and squealer tip geometries. Oil flow visualizations and static pressure measurements on the blade tip, blade surface, and corresponding endwall provide insight to the structure of the two different tip flows. Aerodynamic losses are measured for the different tip arrangements, also. The squealer tip provides a significant decrease in velocity through the tip gap with respect to the flat tip blade. For the flat tip, an increase in Reynolds number causes an increase in tip velocity levels, but the squealer tip is relatively insensitive to changes in Reynolds number.
Previous research has shown that vane clocking, the circumferential indexing of adjacent vane rows with similar vane counts, can be an effective means to increase stage performance, reduce discrete frequency noise, and/or reduce the unsteady blade forces that can lead to high cycle fatigue. The objective of this research was to experimentally investigate the effects of vane clocking in an embedded compressor stage, focusing on stage performance. Experiments were performed in the intermediate-speed Purdue three-stage compressor, which consists of an IGV followed by three stages. The IGV, Stator 1, and Stator 2 vane rows have identical vane counts, and the effects of vane clocking were studied on Stage 2. Much effort went into refining performance measurements to enable the detection of small changes in stage efficiency associated with vane clocking. At design loading, the change in stage efficiency between the maximum and minimum efficiency clocking configurations was 0.27 points. The maximum efficiency clocking configuration positioned the Stator 1 wake at the Stator 2 leading edge. This condition produced a shallower and thinner Stator 2 wake compared with the clocking configuration that located the wake in the middle of the Stator 2 passage. At high loading, the change in Stage 2 efficiency associated with vane clocking effects increased to 1.07 points; however, the maximum efficiency clocking configuration was the case where the Stator 1 wake passed through the middle of the downstream vane passage. Thus, impingement of the upstream vane wake on the downstream vane leading edge resulted in the best performance at design point but provided the lowest efficiency at an off-design condition.
Previous research has shown that vane clocking, the circumferential indexing of adjacent vane rows with similar vane counts, can be an effective means to increase stage performance, reduce discrete frequency noise, and/or reduce the unsteady blade forces that can lead to high cycle fatigue. The objective of this research was to experimentally investigate the effects of vane clocking in an embedded compressor stage, focusing on stage performance. Experiments were performed in the intermediate-speed Purdue 3-Stage Compressor, which consists of an IGV followed by three stages. The IGV, Stator 1, and Stator 2 vane rows have identical vane counts, and the effects of vane clocking were studied on Stage 2. Much effort went into refining performance measurements to enable the detection of small changes in stage efficiency associated with vane clocking. At design loading, the change in stage efficiency between the maximum and minimum efficiency clocking configurations was 0.27 points. The maximum efficiency clocking configuration positioned the Stator 1 wake at the Stator 2 leading edge. This condition produced a shallower and thinner Stator 2 wake compared to the clocking configuration that located the wake in the middle of the Stator 2 passage. At high loading, the change in Stage 2 efficiency associated with vane clocking effects increased to 1.07 points; however, the maximum efficiency clocking configuration was the case where the Stator 1 wake passed through the middle of the downstream vane passage. Thus, impingement of the upstream vane wake on the downstream vane leading edge resulted in the best performance at design point but provided the lowest efficiency at an off-design condition.
Large rotor tip clearances and the associated tip leakage flows are known to have a significant effect on overall compressor performance. However, detailed experimental data reflecting these effects for a multistage compressor are limited in the open literature. As design trends lead to increased overall compressor pressure ratio for thermal efficiency benefits and increased bypass ratios for propulsive benefits, the rear stages of the high-pressure compressor will become physically small. Because rotor tip clearances cannot scale exactly with blade size due to the margin needed for thermal growth considerations, relatively large tip clearances will be a reality for these rear stages. Experimental data have been collected from a three-stage axial compressor to assess performance with three-tip clearance heights representative of current and future small core machines. Trends of overall pressure rise, stall margin, and efficiency are evaluated using clearance derivatives, and the summarized data presented here begin to narrow the margin of tip clearance sensitivities outlined by previous studies in an effort to inform future compressor designs. Furthermore, interstage measurements show stage matching changes and highlight specific differences in the performance of rotor 1 and stator 2 compared to other blade rows in the machine.
This paper covers a comprehensive forced response analysis conducted on a multistage compressor and compared with the largest forced response experimental data set ever obtained in the field. The steady-state aerodynamic performance and stator wake predictions compare well with the experimental data, although losses are underestimated. Coupled and uncoupled unsteady simulations are conducted on the stator–rotor configuration. It is shown that the use of a decoupled method for forced response cannot yield accurate results for cases with strong inter-row interactions. The individual and combined contributions of the upstream and downstream stators are also assessed. The downstream stator is found to have a tremendous impact on the forced response predictions due to the constructive interactions of the two stator rows. Finally, predicted mistuned blade amplitudes are compared to mistuned experimental data. The average amplitudes match the experiments very well, while the maximum response amplitude is underestimated.
The frequency mistuning that occurs due to manufacturing variations and wear and tear of the blades has been shown to significantly affect the flutter and forced response behavior of a blade row. While tuned computational fluid dynamics (CFD) analyses are now an integral part of the design process, designers need a fast method to evaluate the localized high blade responses due to mistuning. In this research, steady and unsteady analyses are conducted on the second-stage rotor of an axial compressor, excited at the first torsion vibratory mode. A deterministic mistuning analysis is conducted using the numerical modal forces and the individual blade frequencies obtained experimentally by tip timing data. The mistuned blade responses are compared in the physical and traveling wave coordinates to the experimental data. The individual and combined impacts of frequency, aerodynamic, and forcing function perturbations on the predictions are assessed, highlighting the need to study mistuned systems probabilistically.
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