The pressure for saving water by closing the water loops in mineral processing is increasing continuously. The drivers for higher recirculating rates include water scarcity in dry areas, environmental legislation that is becoming stricter in most countries, limitations set for wet tailings management and the increased demands for social licenses to operate. At the same time, to make mineral processing sustainable, the recovery of valuable minerals should be maximized. This leads for a need to close the process water circulation. To see the effect of closed water circulation on metallurgical performance, flotation tests were carried out with nickel concentrate thickener overflow water before and after the process of water purification by dissolved air flotation (DAF). Both total nickel recovery and concentrate grade in laboratory scale flotation tests to the Ni rougher-scavenger concentrate increased after DAF treatment. Chemical and mineralogical characterizations revealed that after DAF treatment, the process water contained fewer metal hydroxides and less fine-grained silicate mineral particles, which is most likely the reason for the improvement in the nickel flotation performance. Based on the feasibility study, improved nickel recovery by DAF treatment of process water can bring economic benefits at a concentrator plant.
This paper investigated the effect of mineral surface oxidation on the floatability of Kevitsa low-grade Ni-Cu ore. Physicochemical measurements, ethylene diamine tetra acetic acid (EDTA) extraction, and oxygen uptake experiments were carried out with slurry and recycled process water samples obtained from the Kevitsa Cu-Ni sequential concentrator plant. The pH of recycled process water, copper flotation feed, and nickel flotation feed dropped by 0.7, 0.4, and 0.7 points, respectively, from May to July. The oxygen demand increased from recycled process water to the copper flotation feed, then dropped for the nickel flotation feed. The nickel flotation feed Redox potential (ORP) was lowest for July, while EDTA extractable metals increased from May to July. There was a 20% drop in nickel recoveries from May to July. Based on ORP measurements of the nickel flotation feed, good nickel flotation takes place in a moderately oxidizing (75–170 mV) and alkaline (9.2–9.7 pH) environment. Therefore, the ORP/pH of the nickel flotation feed is important to the nickel flotation. The results showed that at the Kevitsa plant, the grinding process is an electrochemically active environment, which, together with the incoming recycled process water quality, defines the degree of mineral surface oxidation for flotation. The increasing corrosiveness of the recycled process water increased mineral surface oxidation and depressed pentlandite flotation. Laboratory flotation experiments confirmed the observed poor plant flotation response when the corrosiveness of recycled process water increased. Total dissolved solids (TDS) was proven to be a reliable online parameter for the corrosiveness of the recycled process water and was inversely proportional to the pentlandite recovery. The findings of this study may help the plant develop ways to enable a timely response to changes in recycled process water quality to prevent harmful impacts on pentlandite flotation.
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