All Days 2012
DOI: 10.2118/162852-ms
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Unique Solution to Repair Casing Failure in a HTHP Wellbore Allows for Successful Multi-Stage Stimulation Treatment in an Unconventional Reservoir

Abstract: Horizontal shale completions require multi-stage high-pressure hydraulic fracturing stimulation treatments in order to deliver commercially viable production in low permeability reservoirs. Unconventional shale plays, such as the Eagle Ford and Haynesville Shale, often can require stimulation treatments that must be implemented in high pressure and high temperature (HPHT) conditions. Typically, these wells are completed with long casing strings, and it is critical that these monobore casing strings withstand h… Show more

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Cited by 3 publications
(1 citation statement)
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“…Nine total stages were successfully stimulated, allowing the well to become productive. (Wellhoefer, B., et al, 2012) In a collection of eight wells in East Texas, an operator wanted to run swellable packers to perform a short-term temporary application for chemical injection. The operator planned to run swellable packers to perform a chemical injection in the annulus, and then, to pull the tubing and unseat the packers in six months to pull the tubing out of the hole.…”
Section: Case Historiesmentioning
confidence: 99%
“…Nine total stages were successfully stimulated, allowing the well to become productive. (Wellhoefer, B., et al, 2012) In a collection of eight wells in East Texas, an operator wanted to run swellable packers to perform a short-term temporary application for chemical injection. The operator planned to run swellable packers to perform a chemical injection in the annulus, and then, to pull the tubing and unseat the packers in six months to pull the tubing out of the hole.…”
Section: Case Historiesmentioning
confidence: 99%