1994
DOI: 10.2172/10140805
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TMI-2 Vessel Investigation Project integration report

Abstract: The Three Mile Island Unit 2 (TMI-2) Vessel Investigation Project (VIP) was an international effort that was sponsored by the Nuclear Energy Agency of the Organization for Economic Cooperation and Development. The primaiy objectives of the VIP were to extract and examine samples from the lower head and to evaluate the potential modes of failure and the margin of structural integrity that remained in the TMI-2 reactor vessel during the accident. This report presents a summary of the major findings and conclusio… Show more

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Cited by 47 publications
(29 citation statements)
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“…During attempts to unclog a pipe leading from the full-flow demineralizers downstream of the condenser, the accident was initiated by a shutdown of secondary feedwater flow due to a trip of the condensate booster pumps followed by a trip of the feedwater pumps. Best estimates for plant data and events during the accident, as obtained from various post-accident evaluation programs, 6 are depicted in Figure 2 , the steam generator boiled dry; and the resultant reduction of primary-to-secondary heat exchange caused the primary coolant to heat up, surge into the pressurizer, and increase the primary system pressure. The Pilot Operated Relief Valve (PORV) opened to relieve pressure when the RCS pressure reached 15.7 MPa.…”
Section: Synopsis Of Accidentmentioning
confidence: 99%
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“…During attempts to unclog a pipe leading from the full-flow demineralizers downstream of the condenser, the accident was initiated by a shutdown of secondary feedwater flow due to a trip of the condensate booster pumps followed by a trip of the feedwater pumps. Best estimates for plant data and events during the accident, as obtained from various post-accident evaluation programs, 6 are depicted in Figure 2 , the steam generator boiled dry; and the resultant reduction of primary-to-secondary heat exchange caused the primary coolant to heat up, surge into the pressurizer, and increase the primary system pressure. The Pilot Operated Relief Valve (PORV) opened to relieve pressure when the RCS pressure reached 15.7 MPa.…”
Section: Synopsis Of Accidentmentioning
confidence: 99%
“…The event differed from a typical small break LOCA in that the pressurizer liquid level remained high. This was incorrectly interpreted by the reactor operators 4,6 as indicating that the RCS was nearly full of water, when in fact, the RCS was continually losing its water inventory. Emergency core cooling was reduced by operators to address their concerns about a full RCS.…”
Section: Synopsis Of Accidentmentioning
confidence: 99%
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“…In the TMI-2 accident, the hot spot in the lower head vessel was generated by corium attack in spite of water existence in the lower plenum of the reactor vessel [37].…”
Section: Corium Interaction With Lower Head Vesselmentioning
confidence: 99%
“…However, the molten core material did enter the instrumentation tube central chamber and penetrate significant distances outside the reactor vessel. The water inside the annulus between the ICI nozzle and the thimble tube was important for the integrity maintenance of the reactor vessel penetrations, which did not result in any failure of penetration in the TMI-2 accident [37].…”
Section: Lower Head Penetration Integritymentioning
confidence: 99%