2003
DOI: 10.1016/s0022-3115(03)00176-4
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The EFTTRA-T3 irradiation experiment on inert matrix fuels

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Cited by 57 publications
(19 citation statements)
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“…The calculated dissolution curves for MgO under this assumption are plotted as dashed lines in both Figure 16 and Figure 20(a). For the dissolution test conducted at 60 C with magnetic bar stirring in both HNO 3 and H 2 SO 4 , the experimental data follow the calculated curves, suggesting that the proposed model is a good estimate. While for the one conducted at 60 C in ultrasonic bath, the last measured data point falls below the calculated curve, which is probably due to inefficient agitation causing a diffusion barrier to form and slow down the process.…”
Section: Dissolution Behavior Of Mgo-nd 2 Zr 2 O 7 Compositessupporting
confidence: 57%
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“…The calculated dissolution curves for MgO under this assumption are plotted as dashed lines in both Figure 16 and Figure 20(a). For the dissolution test conducted at 60 C with magnetic bar stirring in both HNO 3 and H 2 SO 4 , the experimental data follow the calculated curves, suggesting that the proposed model is a good estimate. While for the one conducted at 60 C in ultrasonic bath, the last measured data point falls below the calculated curve, which is probably due to inefficient agitation causing a diffusion barrier to form and slow down the process.…”
Section: Dissolution Behavior Of Mgo-nd 2 Zr 2 O 7 Compositessupporting
confidence: 57%
“…The ultrasonic power was recorded from three individual tests and averaged to be 10.3 W/s. As discussed before, however, the dissolution rate of MgO was not increased by ultrasound compared with static dissolution, and Nd 2 Zr 2 O 7 didn't dissolve in HNO 3 . The inefficiency of ultrasonic dissolution of MgO is probably due to the size of the composite and its porous structure developed during dissolution.…”
Section: Effects Of Agitation Methods and Dissolution Temperature On Dmentioning
confidence: 67%
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“…While initially favored as a leading candidate and pursued in many research programs, irradiation experiments show that Spinel is likely not a suitable matrix candidate, as it shows large swelling, pellet fracturing, and high fission gas release [Neeft et al, 2003 andMeyer, 2006]. While fission gas release into the inner part of the fuel assembly is not a concern given that the fuel assemblies are vented, it does contribute to fuel swelling due to poor diffusion of the fission gases through the Spinel matrix.…”
Section: Selection Of An Appropriate Inert Matrix Fuelmentioning
confidence: 99%
“…A recent irradiation experiment on inert matrix fuels was conducted in order to compare the irradiation performance among several IMF options, and MgO was shown to be one of the top performers [Neeft et al, 2003]. With the MgO inert matrix, the Pu and MA could be either in the form of simple binary oxides or hosted in a zirconia-based phase, e.g.…”
Section: Selection Of An Appropriate Inert Matrix Fuelmentioning
confidence: 99%