55th AIAA Aerospace Sciences Meeting 2017
DOI: 10.2514/6.2017-1062
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Study on a Long-time Operation Towards Rotating Detonation Rocket Engine Flight Demonstration

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Cited by 19 publications
(22 citation statements)
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“…Mass decrease was determined by electric balance or the decrease in internal tank pressure. For some longer-duration tests, mass flow rate calibration was done [19,29,30]. Actual mass flow rate _ m could be calculated by…”
Section: Outside Insidementioning
confidence: 99%
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“…Mass decrease was determined by electric balance or the decrease in internal tank pressure. For some longer-duration tests, mass flow rate calibration was done [19,29,30]. Actual mass flow rate _ m could be calculated by…”
Section: Outside Insidementioning
confidence: 99%
“…The propulsive performance of RDE and PDE have been widely investigated by many institutions [6,7,9,[12][13][14][15][16][17][18][19][20][21][22][23]29,30]. Kindracki et al [12] measured the thrust and specific impulse of RDE under 0.5 bar.…”
mentioning
confidence: 99%
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