2015
DOI: 10.2118/171806-pa
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Simulation of Residual Oil Saturation in Near-Miscible Gasflooding Through Saturation-Dependent Tuning of the Equilibrium Constants

Abstract: Summary Conventional miscible or near-miscible gasflooding simulation often overestimates oil recovery, mostly because it does not capture a series of physical effects tending to limit interphase compositional exchanges. Those can include microscopic bypassing of oil situated in dead-end pores or blocked by water films, as well as macroscopic bypassing caused by subgrid-size heterogeneities or fingering. We here present a new engineering solution to this problem in the near-miscib… Show more

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Cited by 9 publications
(2 citation statements)
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“…Despite such favorable conditions, residual oil is still expected in the pilot area (Patacchini, Duchenne, Bourgeois, Moncorgé, & Pallotta, 2015) Although the GIP's main purpose was not pressure maintenance, pressure increases of 600 to 800 psi were observed in the wells located in a 4 -5 km range; as soon as GIP ceased, pressures in the wells started to drop, as can be seen in Figure 8 where combined BHCIP of three wells located in the GIP area are shown. The pilot injection wells started in 2001 and were shut-in at the end of 2009 as a result of maturity in terms of operation and data acquisition.…”
Section: Down-flank Gas Injection Pilotmentioning
confidence: 99%
“…Despite such favorable conditions, residual oil is still expected in the pilot area (Patacchini, Duchenne, Bourgeois, Moncorgé, & Pallotta, 2015) Although the GIP's main purpose was not pressure maintenance, pressure increases of 600 to 800 psi were observed in the wells located in a 4 -5 km range; as soon as GIP ceased, pressures in the wells started to drop, as can be seen in Figure 8 where combined BHCIP of three wells located in the GIP area are shown. The pilot injection wells started in 2001 and were shut-in at the end of 2009 as a result of maturity in terms of operation and data acquisition.…”
Section: Down-flank Gas Injection Pilotmentioning
confidence: 99%
“…Significant hysteresis occurs during WAG injection between imbibition and secondary drainage, and these effects, along with three-phase flow, must be correctly represented (Jerauld 1997). Laboratory experiments observed that bypassed oil occurs even after miscible flooding, and accurate computation of residual oil to miscible flood (S orm ) is crucial for correct recovery estimation (Hiraiwa et al, 2007;Bourgeois et al, 2011;Patacchini et al, 2015). Moreover, the timing of gas and WAG injection should be defined after robust screening, as early gas injection will result in poor volumetric sweep efficiency, whereas late injection will result in very low oil production rate (Jerauld et al, 2000).…”
Section: Introductionmentioning
confidence: 99%