Day 1 Tue, October 25, 2022 2022
DOI: 10.2118/206952-ms
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Investigation of an Unexpected Flow Event for a Duvernay Artificial Lift System and Optimization for Future Installation

Abstract: This paper summarizes the work of a client project investigating an "unexpected flow phenomenon" observed for an operational downhole jet pump installed in a deep, high-pressure, light hydrocarbon-condensate well in the Duvernay region of Western Alberta. The jet pump appeared to allow the well to produce multiphase condensate, water, and Non-Condensable Gases (NCGs) without the injection of power fluid. Due to a lack of understanding of the cause of this phenomenon, the well production rate could not be predi… Show more

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