Day 3 Thu, March 24, 2022 2022
DOI: 10.4043/31553-ms
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Holistic Analysis, Diagnostics and Operating Philosophy for Wellhead Leak Issue for Gas Producer, Offshore Malaysia

Abstract: Since the beginning of production, well NA2 and NA3 wells had issues with wellhead integrity due to thermal growth and wellhead tilting. Seepage was observed from wellhead and based on gas chromatography test, the seepage is Synthetic Based Mud (SBM), possibly from B and C annulus (intermediate and surface casing). For well NA3, seepage was observed coming out from the connection of Casing Head and Drive Pipe Housing House (DPHH) while for Well A2, seepage was found between DPHH and conductor. The issues arise… Show more

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“…However, it is difficult to measure the wellbore leakage in high-pressure gas well. Due to high temperature, corrosive fluid, and high stress, well barriers have high probability to leak, including wellhead, 21 tubing string, 11 casing string, 22,23 hanger, 24 cement, 25 and packer or valve. 26 What is more complicated, different well barriers may leak at the same time.…”
Section: Introductionmentioning
confidence: 99%
“…However, it is difficult to measure the wellbore leakage in high-pressure gas well. Due to high temperature, corrosive fluid, and high stress, well barriers have high probability to leak, including wellhead, 21 tubing string, 11 casing string, 22,23 hanger, 24 cement, 25 and packer or valve. 26 What is more complicated, different well barriers may leak at the same time.…”
Section: Introductionmentioning
confidence: 99%