A 3 year, 23 well project drilled by a major operator in Nigeria was challenged to develop methodologies to optimize every aspect of drilling for a development project to reduce total project time and costs.
The team of operator and service company personnel created an approach that systematically examined and challenged the efficiency of all tasks. They then developed and implemented innovative methods to save time by both analyzing repetitive, lengthy, or troublesome operations and challenging many status quo rig activities. The culture of continually challenging the causes of invisible lost time (ILT) that developed resulted in the creation of several critical performance improvement methodologies each of which are explained in detail.
The multiple focus areas where process improvements were made included hole cleaning efficiencies, optimizing the ROP to deliver shortest well time from drilling out the casing shoe to landing the next casing, anti-collision practices to drill out conductors with a separation factor of less than 1.0, BHA design efficiencies for equipment standardization and faster make up and break down times, managing differential sticking risks, improving survey times, and developing best practices to side-track with a point-the-bit Rotary steerable system. Exact times were tracked to establish the required baselines and drilling optimization services were introduced to modify the drilling practices to reach the technical limit.
The technical limit for ROP was achieved and best practices developed in this environment for effective hole cleaning, ease of tripping, and improved tripping speeds of the BHA at the end of every run saved 38.25 days over 15 wells. Average ROP's were improved by 48% in the 17 ½" section and 57% in the 12 ¼" section. The new anti-collision methodology saved 5 hours per well. BHA assembly and tool download efficiencies saved 11.47 days. Wellbore strengthening techniques prevented seepage losses and reduced stuck pipe events. Surveying improvements saved 11.78 days and new sidetracking practices saved 5 hours per sidetrack. Tasks that could be done in parallel to the critical path were identified and tasks on the critical path were performed more efficiently. ILT elimination in drilling processes saved a total of 96 days of rig time over an established performance baseline during this 23 well project. The operator set two records for the fastest drilled and completed conventional offshore wells in Nigerian history.