2011
DOI: 10.1088/0029-5515/51/3/033007
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A new disruption mitigation valve (DMV) and gas flow in guiding tubes of different diameter

Abstract: A new disruption mitigation valve, the DMV-30, has been developed and tested. The orifice output area of the valve is a factor of 2.4 and 12.25 times larger than that of its predecessors, DMV 20 and DMV 10, and the gas reservoir amounts to 1.3 l while the older version used at JET had only 0.65 l. The coil which provides the magnetic field pulse for the activation of the piston by an eddy current is outside of the working gas volume such that now all gas volumes are now made of stainless steel. The valve has t… Show more

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Cited by 25 publications
(15 citation statements)
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“…The flow model was validated with available measurements of a TEXTOR-like injection system [13,14]. At the same time the calibration set from [13] was improved due to a more suitable processing The model correction factor was found to depend on the ratio of the orifice area to the delivery tube area.…”
Section: Discussionmentioning
confidence: 99%
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“…The flow model was validated with available measurements of a TEXTOR-like injection system [13,14]. At the same time the calibration set from [13] was improved due to a more suitable processing The model correction factor was found to depend on the ratio of the orifice area to the delivery tube area.…”
Section: Discussionmentioning
confidence: 99%
“…The 10 and 18 mm valves were calibrated with the 38 mm tube, while the 28 mm valve was used with both For the tests of the 28 mm valve a commercially available interferometer was employed, whereas for the 10 and 18 mm valves a self built interferometer was used. In the latter case the processing procedure has recently been significantly improved with respect to [13,14]. Since the improvements result in a noticeable change of the pulse form, first a short reanalysis of the data for the 10 and 18 mm valves is presented below.…”
Section: Laboratory Calibration Of the Flow Modelmentioning
confidence: 99%
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“…Figure 5b gives the number of particles injected before start of the current quench , as calculated from adiabatic expansion into vacuum. This approach has been validated with lab measurements using the JET set-up [18,19,20]. The fraction of gas injected before the current quench , decreases with increasing pressure because of the shorter cooling phase.…”
Section: Pre-thermal-quench Phasementioning
confidence: 99%
“…The design of the MGI valve presented here is largely based on previous designs deployed on TEXTOR, ASDEX upgrade, and JET [1][2][3], with considerations made for operation in the ITER environment.…”
Section: Introductionmentioning
confidence: 99%